ISSN:1003-8620

CN:42-1243/TF

Governed by: CITIC Pacific Special Steel Group Co., LTD

Sponsored by: Daye Special Steel Co., LTD.

Special Steel ›› 2023, Vol. 44 ›› Issue (1): 15-18.DOI: 10.20057/j. 1003-8620.2022-00035

Special Issue: 硫磷氧的控制

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Production Practice of 90 t BOF⁃RH⁃CC Process for ZG⁃12 Ultra⁃low Phosphorus Steel

Yang Limei1 ,Yin Chuanlei1,Ma Qingfeng2 ,Zhai Wanli1 ,Liu Congde2 ,Zuo Hui1   

  1. 1 Technology Center;2 Steelmaking Works,Huaigang Special Steel Co.,Ltd.,Jiangsu Shagang Group,Huai'an 223002
  • Received:2022-05-13 Online:2023-02-01 Published:2023-01-20

ZG-12超低磷钢90 t BOF-RH-CC工艺的生产实践

杨丽梅1 ,印传磊1,马庆丰2 ,翟万里1,刘从德2 ,左   辉1   

  1. 江苏沙钢集团淮钢特钢股份有限公司 1 技术中心;2 炼钢厂,淮安 223002
  • 作者简介:杨丽梅(1990-) ,女,硕士,工程师;

Abstract: In the light of problems of smelting ultra-low phosphorus steel (%/: <0. 03C、<0. 01 OP、<0. 015S、< 0.06Mn、vO. 02Cr、<0.02Ni), the lower liquid temperature at 90 t BOF tapping and serious overoxidation of liquid, led to heating refining by LF, are tested and studied by process optimization. The results show that during BOF (0. 018% - 0. 025% P) tapping process by adding lime and refining slag to produce slag with binary alkalinity 7 and P2O5 <0.5%, the dephosphorization rate of liquid in ladle reaches up to 75%, the phosphorus content of finished products is less than 0.010%, the smelting time is shortened by 3 ~ 4 min. At the same time, the dephosphorization rate of ladle decreases with the increase of liquid steel temperature at the end of converter blowing, the BOF optimum end-point temperature is between 1 630 °C and 1 655 °C. By adopting ladle dephosphorization technology, the smelting process of ultra-low phosphorus steel is shortened to converter blowing—►RH treatment—►continuous casting, and the LF refining process is omitted.

Key words: Ultra?Low Phosphorus Steel, Ladle, Slag, Dephosphorization in BOF Tapping Process

摘要: 对钢厂采用90 t转炉冶炼超低磷钢(%/:<0.03C,<0.010P,<0.015S,<0.06Mn,<0.02Cr,<0.02Ni),转炉终点钢液温度偏低、过氧化严重,需经过LF升温精炼等问题,进行了工艺优化试验研究,结果表明:转炉(0.018%~0.025%P)出钢过程中使用石灰和精炼渣,形成二元碱度为7、<0.5%P2O5炉渣,可使钢包钢水脱磷率达到75%,成品磷含量低于0.010%,冶炼时间缩短3~4 min。同时,转炉吹炼终点钢液温度升高,钢包脱磷率呈降低趋势,转炉最佳终点温度为1630~1655℃。通过采用钢包精炼脱磷技术,超低磷钢冶炼流程缩短为转炉吹炼→RH处理→连铸,减少LF精炼工序。

关键词: 超低磷钢, 钢包, 炉渣, 转炉出钢过程脱磷